All posts by Adam

Wessex Safety Hour – 1st May 2018

Safety Hour Attendance Last Week – 97%  (Target = 67%)

Close Calls Raised – 60  (Target = 146)

% of Close Calls in <90’s – 92%  (Target = 85%)

 

Incidents last week

14/04/2018
Hersham
Irregular Working Item 39
The Engineering Supervisor tor T3 possession Item 39 was advised by the plain line tamper crew that there were two members of staff surveying the track on the Up Slow Cess.
The ES was not aware of this, as the staff had not signed into their worksite.
It was believed that the staff were watchman for the Sink Hole incident.
This incident was subject to further investigation.
14/04/2018
New Malden
Possession Irregularity Item 39
The PICOP for T3 possession Item 39 reported that the straps had been placed incorrectly on the Up Slow/Fast at 10m 12ch vice 10m 01ch.
The irregularity was realised upon the Driver of tamper 6Z03 who stopped short of them.
This incident was subject to further investigation.
14/04/2018
Rowlands Castle
Staff accidents x2
Two members of Havant PWay staff were sprayed in the face with hydraulic fluid whilst removing a hose from a track stressing kit.
First aid was administered and the Golden Hour was applied.
The staff suffered no ill effects.
16/04/2018
Woking
Staff accident Incident
While reversing the van to park it at the Depot, a Track Quality Supervisor accidentally hit a skip. There was minor damage to the rear door, but no injuries.
The Golden Hour was applied for chain of care.
17/04/2018
Byfleet and New Haw
Staff accident Incident
A Woking PWay Technician was walking back through an alleyway with his team after giving up a T3 possession when his ankle gave way causing it to twist.
He had experienced he same injury 1 month previous.
The Golden Hour was applied and no lost time was anticipated.
18/04/2018
Epsom
Line Block Irregularity
A Line Block irregularity took place when the Signaller granted the authority number to the COSS to start work and then realised that a South West Railway service (2D38) was still in section and asked the COSS to stand clear.
The train concerned had been beyond the workgroup at the time, but within the blocking limits.
This incident was subject to further investigation.
19/04/2018
Wimbledon Park Depot
Possession Irregularity – Item 506
The South West Railway Wimbledon Park Depot Performance Manager reported that a marker board for the possession on no.1 road had been placed in a different position to the previous night (at the Earlsfield Exit).
Upon investigation, it was confirmed that an error had been made by a Possession Support Staff member from the Clapham PWay.
This incident was subject to further investigation.
19/04/2018
Eastleigh
Staff Accident
A member of the Outer Ultrasonic team received a shoulder injury whilst lifting Ultrasonic equipment.
The Golden Hour was applied and there was no lost time.
19/04/2018
Datchet
Staff Accident
A member of Feltham S&T twisted their left ankle whilst walking on ballast.The ankle became sore, but there was no immediate bruising or swelling.
The Golden Hour was applied and there was no lost time.
22/04/2018
Fratton
Damaged AWS for HT55 Signal Incident
A Track Quality Supervisor reported that a Tamper working within T3 possession Item 91 had damaged the AWS for HT55 signal at 44m 3ch.
The AWS was unreliable and trains cautioned post the T3 being given up until a temporary solution was put in place.
This incident was subject to further investigation.
25/04/2018
Milford
Staff Accident
A member of Havant S&T trapped their finger when opening a location cabinet door.
The Golden Hour was applied and there was no lost time.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 9th April 2018

Safety Hour Attendance Last Week – 62%  (Target = 67%)

Close Calls Raised – 34  (Target = 146)

% of Close Calls in <90’s – 91%  (Target = 85%)

To dial 111 (NHS) or 101 (non-emergency police) from a mobile, prefix with a 9 – 9111 or 9101.
To dial 111 (NHS) or 101 (non-emergency police) from a desk phone, prefix with a 91 – 91111 or 91101.
999 (or 112) can be dialled directly

Number Mobile Phone Desk Phone
999 Emergency 999 999
101 Non-emergency police 9101 91101
111 NHS 9111 91111

 

Incidents last week

26/03/2018
Clapham Junction / Berrylands
Possession Irregularity (Item 42)
The PICOP of item 42 reported that 6N03 had left the worksite with no certificate of readiness (to confirm that the load was in gauge and secure).
This incident is subject to further investigation.
27/03/2018
Boxhill
Irregularity Line Blockage
Wimbledon P-Way reported that they had a line blockage irregularity after the COSS had mixed up their mileages.
They had a Line Blockage between 18m 45ch – 18m 20ch, but meant to take it between 20m 69ch – 20m 68ch.
As they got halfway across the River Mole bridge, they became aware of a train approaching and were able to reach a position of safety.
This incident is subject to further investigation.
31/03/2018
Blackwater
Cows struck
A GSMR Emergency Rec call was made by 2O53 (Great Western Railways) to report a herd of cows in the cess on the Up line, one of which had been swiped by the train.
Upon the MOM attending, the cows were returned back into their field and a broken fence line was repaired.
03/04/2018
Waterloo
Staff accident
An Operations Delivery Manager was involved in a multi-vehicle RTA near the Shell Building and sustained injuries to the neck, back, head and shoulders. There were no broken bones.
The Golden Hour was applied and this became a lost time injury.
03/04/2018
Hinton Admiral / Christchurch
Tree cut down in front of 1W17
1W17 reported that the train had just ran over a section of tree which had just been cut by tree fellers.
The Driver was very shaken by the event, but there was no damage to the train.
Upon investigation it was established that trees were being cleared by Works Delivery staff (Off Track).
This incident is subject to further investigation.
04/04/2018
Hounslow
Staff assault
Feltham S&T reported a male trespasser crossing between platforms 1 and 2 shouting abuse, filming them.
As time went on, the male then started spraying graffiti and became physically violent with the S&T when challenged.
The male was later detained by the police.
05/04/2018
Emsworth
Staff Accident
An Outer Delivery Unit Section Manager [Rail Testing & Lubrication] was stationary waiting for a vehicle to turn right into Sandy Lane from the A334, when he heard heavy braking from behind and was struck on the off side rear by a large van.
The Golden Hour was applied and the injuries are to be confirmed.
08/04/2018
Aldershot
Worksite Irregularity
Tamper 6J61 was given authority by a McGinley Engineering Supervisor to travel through a worksite at caution within T3 Possession Item 116, but came across 2111 points set against them and stopped short.
The ES admitted their error, but was permitted to continue.
The Till Dawn process had not been in place on this line as it was a single transit movement.

Material

Safety Advice – Emegency Numbers

Cable theft appears to be on the rise.  If you see anything suspicious, please report to the WICC or BTP on 0800 40 50 40

 

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 26th March 2018

Safety Hour Attendance Last Week – 74%  (Target = 67%)

Close Calls Raised – 42  (Target = 146)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

18/03/2018
Kingston
RRV Derailment
An RRV had derailed at F625 points within a T3 engineers possession caused by the adverse weather conditions and a build-up of ice.
The RRV was re-railed and the only damage sustained was to an insulating pot.
This incident was subject to further investigation.
18/03/2018
West Drayton
Staff Accident
A Section Manager at Feltham had a low speed collision whilst driving onto the slip road to join the M4 when the vehicle in front braked unexpectedly.
Both vehicles sustained minor damage, but there were no injuries.
The Golden Hour was applied for chain of care.
18/03/2018
Windsor and Eton Riverside
Signaller Error – 10 coaches signalled onto 5 coaches
The Signaller had been dealing with track failures within Windsor and had not been aware that a train had been spilt (as booked) leaving 5 coaches behind.
The Signaller then cautioned the next 10 coach arrival to pass the signal at danger only for the Driver to see the other train still in the platform.
The train was arranged to return back behind the signal and be re-platformed.This incident was subject to further investigation.
18/03/2018
Woodsford No 38
Car on the Line
A member of public reported that they had a car accident, struck Woodsford No 38 crossing and the car was on the track.
An emergency switch off was arranged.
The MOM arrived on site and having made an assessment, advised that the car was clear of the railway and it was safe to run trains.
There were no track issues identified, but the S&T had to repair the damage caused to their equipment.
18/03/2018
Dorking
Staff Accident
Whilst driving along a country lane, a member of Wimbledon PWay slid and skidded on ice/snow and careered to the right hitting the curb.
They tried to correct the skid, but ended up veering to the left and going down a bank into a bush.
The Golden Hour was carried out and apart from being shaken, there were no injuries.
20/03/2018
Rowlands Castle
Cat A SPAD 2P50
South Western Railway service 2P50 reported passing HT18 signal at danger without authority by up to two coach lengths.
The signal had been at danger due to a signalling failure caused by a cable theft attempt and Emergency Special Working being in place.
The Driver made no allegation against the signalling equipment or unit.
This incident was subject to further investigation.
21/03/2018
Wokingham
Member of the Public Injured
A Member of the Public was struck by 3 blue poles on the leg that slid from the top of stairs leading to a track access gate on 20/03/2018. (Emmbrook Road, bridge 19/1383, RDG2).
Upon inspection, there were up to 50 other poles connected to some project / engineering work and the 3 that fell had not been secure.
This incident was subject to further investigation.
22/03/2018
Waterloo
Waterloo P17 – Passenger Accident
A member of the public was running to catch a train, but fell between the train and the platform edge.
They were helped back onto the platform by other members of the public, but they had noticeable blood within their mouth and was left in the care of platform staff.
No trip hazards were identified.
22/03/2018
New Malden
Staff Accident
A member of PWay staff pulling on rail fastenings, fell back when the hook used to do this slipped out.
The member of staff fell back onto another colleagues left leg awkwardly causing immediate pain.
The Golden Hour was applied and although there were no broken bones, the injury became lost time.
23/03/2018
Weybridge
Track Noise/Defect 2F10
At 06:43 South Western Railway service 2F10 reported hearing a noise from the Up Fast line as 2P96 was travelling through the section.
2 further trains were cautioned and reported nothing amiss, so the Signaller returned to normal working prior to required PWay attendance.
At 10:14 2F24 (the same driver as 2F10 earlier), further reported a ‘scoop’ of rail missing from the nearside rail at the same location.
Trains were then diverted around the defect until a rail clamp was applied.This incident was subject to further investigation.
23/03/2018
Lightwater
Staff Accident (RTA)
A Senior Project Engineer was the 3rd car back from a roundabout turning onto the M3.
The 1st car moved away and the 2nd car appeared to pull away too, but then stopped leading to a slow speed rear end collision.
There were no injuries.
The Golden Hour was applied for chain of care.
25/03/2018
Feltham
Vehicle Damage / Accident
A member of Feltham S&T damaged the work van by scrapping a wall/barrier when driving too close to the gate key pad.
There were no injuries and Chain of Care was carried out.
25/03/2018
Bedhampton Level Crossing
RRV Oil Leak
An RRV working within T3 item 76A engineers possession experienced a burst hose and lost approximately 2 litres of hydraulic oil onto the track.
The majority of the spill was contained and cleaned.
A further incident then occurred as the machine was lifting a trailer off of the track where a further 180 litres of fluid was lost. The majority of which was contained in buckets and by spill kits. Approximately 5 Litres reached the ground.
This incident was subject to further investigation.
25/03/2018
Raynes Park
Safety Incident
A PWay Section Manager reported staff  had advised them that a metal ‘J Bar’ which is placed through holes in wheel timbers and interlocks with other ‘J Bars’ and tightened with nuts had fallen off an embankment by bridge 33, landed on the roof of a car smashing the sunroof.
No-one was in the vehicle and a search was carried out to find the owner without success.
A note was left on the windscreen.
This incident was subject to further investigation.
25/03/2018
Raynes Park
Staff Accident
A Contractor working for Works Delivery was carrying a Strail unit as part of a 4 man lift when they slipped over and the Strail unit landed on their left leg causing bruising.
They were assisted back to the welfare unit to be checked over. His leg was sore, but was able continue to do light duties (no lifting).
The onsite lead arranged for them to be taken home as a precaution and to report to work tomorrow morning to possibly be given light duties.
The Golden Hour was applied.
26/03/2018
Eastleigh West Junction / Portchester
Possible Possession Irregularity – Item 106
The Outer ODM reported that whilst Possession Support Staff were removing protection to shorten Item 106 from Part 1 to Part 2, one detonator appeared to have been exploded beyond No 10Pts in Back Road No1 some time between 01:09 and 23:32.
Investigations are ongoing.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 19th March 2018

Safety Hour Attendance Last Week – 78%  (Target = 67%)

Close Calls Raised – 86  (Target = 146)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

13/03/2018
Worting Junction
Staff Accident
A member of Eastleigh Distribution and Plant slipped on the uneven ground and twisted their ankle.
The Golden Hour was applied and first aid was given.
The Injured Party later attended hospital where they diagnosed that the ankle may have been fractured.
15/03/2018
Feltham /Ashford
Possession Irregularity – Item 514
A contractor, working for McGinley’s on behalf of Feltham Track Section Manager attempted to strap at the wrong location.
The contractor, who had strapped at this location the previous night, used the track locator app to verify their position due to the poor weather conditions however; they were approximately 2 chain from the correct location.
The contractor tested the conductor rail, but did not follow the process of strapping the running rails first and did not use either rubber gauntlets or short circuiting bar.
When the contractor tried to attach the strap to the conductor rail, the result was the con rail flashing over and causing the electrical breakers to trip.
Chain of care and a follow up investigation then took place.
During the Injured Party’s interview some 2hrs later, he complained of dry eyes and as a precaution, attended hospital where they confirmed that he had not suffered arc eye.
The Golden Hour was applied and no lost time was anticipated.
16/03/2018
Cooks Level Crossing
Staff Accident
A member of Woking PWay was digging some ballast on the track when he hit something hard and jolted his back causing some pain.
The Golden Hour was applied and no lost time was anticipated.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 12th March 2018

Safety Hour Attendance Last Week – 75%  (Target = 67%)

Close Calls Raised – 148  (Target = 146)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

05/03/2018
Havant
Van Door fall off
When leaving the maintenance depot, the Pway van crew sliding door fell off and into the road.
No one was injured and there was no damage to any other vehicles.
It was thought that the mechanism which had been faulty previous to the incident was rectified.
This incident is subject to further investigation.
06/03/2018
Farlington Junction
HT2629 points failure / possession irregularity
Havant ASC reported that HT2629 points would not go back into auto after being in manual during possession Item 84.
Upon investigation it was established that the points had been put onto manual without the Signaller’s knowledge or permission.
This incident is subject to further investigation.
11/03/2018
Hinchley Wood
Staff Accident
A member of Woking PWay staff stepped into a drain gulley and rolled his ankle when getting out of a van.
The injured party experienced a lot of pain and the ankle became swollen.
First aid was administered.
The Golden Hour was applied and this became a lost time injury.
11/03/2018
Wimbledon
2M02 wrong route
South West Railway service 5M02 was offered to depart from No.2 road to arrive in platform 4 at Wimbledon on the LUL side which is restricted from this type of stock.
Arrangements were made for the Driver to be talked out and to run as an empty train to Clapham.
This incident is subject to further investigation.
11/03/2018
Millbrook
Staff Accident
A member of Works delivery staff hand slipped and struck the location cabinet casing when removing old cables. In doing so, they aggravated an old injury.
The hand became swollen and warm to the touch and a cold compress was applied.
The Golden Hour was applied and the injured part was taken to A&E. There were no broken bones and no lost time anticipated.
The injured party had been wearing cat 5 classified gloves which had become wet, oily and contaminated.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 5th March 2018

Safety Hour Attendance Last Week – 62%  (Target = 67%)

Close Calls Raised – 86  (Target = 146)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

27/02/2018
North Sheen Level Crossing
Operational Incident – (Person trapped within crossing)
South West Railway service 2R35 advised the Signaller that a male was stuck within the Level Crossing limits.
The Signaller replaced the signals to danger on the up and down lines as fellow members of public helped the male out.
Upon reviewing the CCTV, it was established that the incident had been a Signaller error and is subject to further investigation.
28/02/2018
Richmond / Strawberry Hill
Item 132 Possession Irregularity
A Trainee Signaller granted signal protection at 00:50hrs for T3 engineering possession item 132 with South West Railway service 2O77 still within possession limits at F91 signal.
No protection had been laid when the error was made.
This incident is subject to further investigation.
28/02/2018
Overton
Staff Accident
A member of Eastleigh PWay was walking from an access gate toward the down line when they slipped on icy underfoot conditions.
The injured party broke their fall with their left arm which became swollen but did not require medical attention.
The Golden Hour was applied and there was no lost time.
28/02/2018
Woking
Staff accident (Low speed RTA)
Whilst stationary in a work vehicle at the station, a Stores Coordinator was struck from behind by another vehicle.
There were no injuries and the Golden Hour was applied for chain of care.
01/03/2018
Woking
Staff Accident (Low speed RTA)
Whilst driving a works van within the South West Railway car park, a member of Telecoms staff turned left down a slight slope and upon applying the brake, the wheels picked up on the ice and slid into the front of a parked car.
There was no damage to the van however; the parked car sustained a crack to the bumper and a dent to the bonnet. There were no injuries.
The Golden Hour was applied for chain of care.
02/03/2018
Haslemere
Staff accident (RTA)
A member of Woking Distribution staff collided with an abandoned parked car that was in the middle of Woolmer Hill Rd. The work van was too damaged to move, but there were no injuries.
Arrangements were made for the recovery of the vehicle and a colleague picked up the Driver.
The Golden Hour was applied for chain of care and there was no lost time.
02/03/2018
Waterloo
Wrong head code – 12 car 450
Due to degraded mode, South West Railway service had been described as 2F24 vice 2F98 in error.
The error was realised before the train arrived at Waterloo on the Up Slow line and arrangements were made to allow the service to arrive in platform 6.
A clear understand was reached between the Signaller and train crew, as the service was formed of 12 coaches and would not be fully accommodated.
02/03/2018
Portsmouth and Southsea
Reported operational incident – 1P33
Due to degraded mode, 1P33 terminated within a low level platform formed of 12 coaches and was not fully accommodated.
The selective door opening system however; only opened doors on the coaches that were within the platform.
04/03/2018
Kew Bridge
Staff accident (RTA)
(Late report) – At 09:35hrs on 02/03/2018, a member of Feltham PWay was driving through an access gate at approximately 5mph in a Network Rail van, but due to the icy conditions the van slid sideways and made contact with the gate post.
Damage was sustained to the left hand side door and the window shattered.
There were no injuries sustained, but Chain of Care was carried out.
The Golden Hour was not applied.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 26th February 2018

Safety Hour Attendance Last Week – 69%  (Target = 67%)

Close Calls Raised – 72  (Target = 146)

% of Close Calls in <90’s – 90%  (Target = 85%)

 

Incidents last week

04/02/2018
Brockenhurst
Staff Accident
A member of Works Delivery staff was changing sleepers when they slipped and fell backwards onto a rail jack.
The Injured Party sustained a graze and no first aid was required.
The Golden Hour was applied and there was no lost time.
05/02/2018
Portsmouth and Southsea
CAT A SPAD 1P59
1P59 passed red signal by 1 coach length.
The Driver made no allegation against the signalling equipment or unit, but stated he was “Reading ahead”.
The Driver did not indicate that they lost concentration.
The train was brought to a stand by TPWS.
06/02/2018
New Malden
Staff Accident
Whilst on W231 signal gantry, a member of S&T missed a step resulting in an ankle sprain.
The Golden Hour was applied and no lost time was anticipated.
07/02/2018
New Malden
Severe arcing over point work
2J53 reported severe arcing going over the point work and upon coming to a stand at Berrylands, a fire then started under the front coach.
The train was evacuated.
08/02/2018
A303
Staff Accident x2 (RTA)
Two members of Works Delivery staff were involved in a head on collision.
Upon attending hospital, one was sent home but the other had a fractured rib cage and a chipped pelvis.
The Golden Hour was applied.
11/02/2018
Fratton
Staff Accident
A team of PWay staff were turning a piece of rail over in the four foot within an engineering T3 possession, but whilst doing this a piece of ballast impeded the rail and it fell back over onto its side, landing onto the left foot of a member of the team.
The foot was examined at hospital which identified that it had been bruised.
The Golden Hour was applied and there was no lost time.
11/02/2018
Southampton Central
2E52 Stopped Short in Platform 3
2E52 stopped short in the middle of platform 3 resulting in the train not being fully accommodated by 2 coaches.No doors were opened.
13/02/2018
Guildford / Farncombe
Possession Irregularity Item 95
The Engineering Supervisor handed back their worksite to the PICOP after arranging to remove 2 sets of straps on the Up Main, but had overlooked two others on the Up and Down Ash at 30m35ch.
The PICOP had not been aware of the oversight, so authorised the Electrical Control Room Operator to close the breakers which resulted in a short circuit. There was minor damage.
Upon further investigation, it was found that 6 sets of straps were left on the track.
14/02/2018
Waterloo
12 Car 450 signalled into Platform 5 – 1P44
1P44 was signalled into platform 5 and the driver has accepted the route in error.
Arrangements were made for the Guard to open the doors from the 8th coach via ASDO, but all 12 coaches released.
No-one was seen to exit the train and arrangements were made for the train to carry out a shunt.
The On Call Guard and Driver Managers were advised and followed up the incident.
The S&T checked the beacon and it was working as designed
15/02/2018
Ryanes Park ECO
Possession Irregularity Item 79
A Raynes Park Electrical Control Room Operator gave permission to the PICOP to test and apply a strap within item 79 on the Up and Down Epsom lines at 8m60ch at Raynes Park.
The test found the conductor rail to be live after the ECO had failed to open 2 circuit breakers.
15/02/2018
Vauxhall
Accident Report
Whilst driving a Network Rail vehicle from Clapham Yard to Waterloo, a PWay track operative was involved in an RTA when a tow truck moved from outer into the inside lane with no warning causing.
Undercover officers witnessed the event and paramedics were called.
The Operative then began to experience pains in his right shoulder and he was advised to see his GP in the morning.
The Golden Hour was applied and no lost time was anticipated.
15/02/2018
Waterloo
2P40 12 car in Platform 6
2P40 was routed as booked into platform 6, but the train was formed of a 12 coach 450 unbeknown to the Signaller.
The front 10 coaches were accommodated and a door release was offered for just those 10.
The On Call Driver and Guards manager were advised.
16/02/2018
Waterloo
12 car 450 stock signalled into platform 7 – 5G64
5G64 formed of 12 car 450 stock as per diagram, was signalled into platform 7 in error vice 13 due to the late arrival of 2P62 required to attach to 1W68.
The On Call Driver Manager was advised and the Driver was relieved.
16/02/2018
St Denys
6Q66 Route Prohibited
The Eastleigh SSM reported that a Matisa Tamping Machine (6Q66) had traversed the Down Line between St Denys and Woolston in error. Matisa Tampers are restricted from using this route.
20/02/2018
Wylye Level Crossing
Staff Accident / Staff Incident
Whilst putting cable into troughing, a team of Works Delivery staff returned to a place of safety for a train to pass at line speed.
The vortex of the train resulted in a hard hat being blown off of one of the teams head and striking another with force on the bottom of the shin on the left leg causing discomfort and bruising.
Upon investigation it was established that the helmet had blown off due to a woolly hat being worn underneath.
The Golden Hour was applied and no lost time was anticipated.
This incident is subject to further investigation.
22/02/2018
Portcreek Junction
Staff Accident
A member of PWay staff experienced pain in the left of his abdomen whilst carrying out a sleeper change and dispersing of ballast with a shovel by means of a twisting action.
The Golden Hour was applied and no lost time was anticipated.
24/02/2018
Salisbury
Suspect Cat A SPAD – SY240 Ground Position light (Late report)
A fault was reported on Wednesday 21/2/18 by the Salisbury Signaller regarding track circuits flooding (failing) following a shunt move beyond SY240 signal involving 5L56.
The S&T have since investigated this and confirmed that they believed a Cat A SPAD to have occurred as no route was set and SY240 signal never displayed a proceed aspect.
The Forward Facing Camera was downloaded by SWR which proved that a SPAD did occur in line with the S&T evidence provided.
25/02/2018
Aldershot North Junction
Staff accident
Whilst unloading/loading an RRV within a work site, a PWay technician caught his leg on the spike used for speed boards and grazed his shin.
The Golden Hour was applied and this became a non-lost time.

Material

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 5th February 2018

Safety Hour Attendance Last Week – 81%  (Target = 67%)

Close Calls Raised – 54  (Target = 146)

% of Close Calls in <90’s – 89%  (Target = 85%)

 

Incidents last week

21/01/2018
Waterloo
Signaller error
Post a regulation error at Waterloo, the Signaller requested that the Driver should change ends and return to Queenstown Road.
Due to a breakdown in communication and a clear understanding not being reached, the Driver began to carry out the movement without first checking with the Signaller once they changed ends.
Upon investigation, it had appeared that the Signaller had not been specific with their instruction.
This incident is subject to further investigation.
23/01/2018
Dean
Staff Accident
A member of Works Delivery staff was lifting the sleeper end by hand when they felt their back spasm.
The Golden Hour was applied and the injured party was able to return to work the following day.
This incident is subject to further investigation where the manual handling technique used will be visited.
23/01/2018
Raynes Park / New Malden
Allegation of unsafe activities lineside
South West Railway service 2G37 reported a member of staff in full PPE walking towards Raynes Park in the Down Slow Cess who did not acknowledge the horn.
A further service (2F37) reported a similar event in the vicinity of a Goals football pitch where the Driver also blew the horn with no acknowledgement. It was also observed that the member of staff was writing things down and texting on a mobile device. After a few more blasts on the horn, they then acknowledged the train.
2K37 was cautioned with a view to stop and identify them, but no-one was seen.
The Safe System of Work was found and the individual was identified.
This incident is subject to further investigation.
25/01/2018
Dunbridge
Staff Accident
Whilst squaring up concrete sleepers, a member of PWay was struck by a jack on the shin which caused bruising.
The Golden Hour was applied and there was no lost time.
25/01/2018
Brockenhurst
Staff Accident
A Gannymead Operative was digging up ballast with a shovel as part of a sleeper change.
Whilst doing so, he lost his footing and turned his right ankle.
His ankle became badly bruised and required a hospital visit.
The Golden Hour was applied and lost time was anticipated.

Material

IP Home Safe 02 Feb 2018

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 29th January 2018

Safety Hour Attendance Last Week – 59%  (Target = 67%)

Close Calls Raised – 55  (Target = 146)

% of Close Calls in <90’s – 92%  (Target = 85%)

 

Incidents last week

14/01/2018
Ashurst
Item 48 Irregularity
A Machine Controller working for Ganymede Solutions left an RRV unattended a couple of times within a T3 engineering work possession and carried out movements without the appropriate authority of the Engineering Supervisor.
This incident is subject to further investigation.
15/01/2018
Eastleigh
Road Traffic Accident
An Outer DU Welder reported that he had an RTA on 08/01/2018 whilst approaching a roundabout at the M27 junction.
A vehicle in front stopped unexpectedly causing him to swerve at the last minute and clip the rear bumper and wheel arch of the other car leaving a scuff mark.
There were no injuries.
The Golden Hour was not applied due to the late report.
17/01/2018
Clapham Junction
Near Miss 5R05
South Western Railway empty service 5R05 reported a near miss with a team of 3 S&T on the Up Windsor Fast line London side of the station.The S&T had been called out to a failure on 663B points situated within the Up Windsor Slow, but during the fault finding process the team begun to focus their attention on the point machine situated between the Up Windsor Slow and Up Windsor Fast putting them in danger of approaching trains.
Having been conscious to rectify the fault, the team overlooked further adequate protection resulting in the Near Miss.
The Golden Hour and Chain of Care was applied to all parties in an exceptional manor.
The incident is subject to further investigation.
Note:Thank you to all those involved in this incident for being transparent with what occurred, as this will allow others who could become exposed in a similar way to learn from your event.
17/01/2018
Woking
Staff Accident
Whilst selecting concrete sleepers within the yard, a PWay Team Leader caught the ‘dunnage’ (wood used to secure the storage of sleepers), resulting in one of them stacked 2 high to fall and trap his ankle against an adjacent sleeper pile.
The injured party attended hospital for an x-ray as a precaution, but apart a graze and bruising, there were no broken bones.
The Golden Hour was applied and this became a Lost Time Injury.

Material

Instructions for working on or near level crossings
Wessex Safety Alert 2018 01 23 – Peters Finger
IP Southern Home Safe 24 Jan 18
Four in five people don’t know how to use a zebra crossing properly

If you would like to raise a question. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

Wessex Safety Hour – 22nd January 2018

Safety Hour Attendance Last Week – 70%  (Target = 67%)

Close Calls Raised – 48  (Target = 146)

% of Close Calls in <90’s – 88%  (Target = 85%)

 

Incidents last week

07/01/2018
Waterloo
Staff Accident
Whilst walking to site, a Strapman working within T3 possession item 7 dropped a short circuiting strap onto a live conductor rail causing a tripping and flashover.
The flashover caused arc eye and he attended hospital where he was administered eye drops.
The Golden Hour was applied and this became a lost time injury.
09/01/2018
Leatherhead
Generator Fire
Stray sparks caused by grinding within T3 possession item 98 caused a generator to catch fire.
As the fire subsided, extinguishers were then used to put it out.
There were no injuries.
This incident is subject to further investigation.
09/01/2018
Clapham Junction
Staff Accident
A PWay Trackman carrying out back filling on a sleeper change within a T3 possession lost his footing stepping over a conductor rail and twisted his right ankle.
He was taken back to the Clapham Yard Maintenance depot and attended the Hospital as a precaution.
The Golden Hour was applied.
Non lost time injury.
12/01/2018
Clapham Junction
Staff Accident (RTA)
A Technician from Clapham PWAY was reversing a Network Rail vehicle within the depot and had a low speed (2-3 mph) collision with another car.
There were no injuries, although the Golden Hour was applied for chain of care.
12/01/2018
Petersfield
Staff Accident
A Lineside Asset Engineer fell on muddy ground and injured their right ankle.
They were to hospital by ambulance and an x-ray found that they had sustained a multiple fracture, ligament damage and a dislocation.
The Golden Hour was applied and this became a lost time Injury.

Material

If you would like to raise a question.  Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.