Wessex Safety Hour – 4th July 2017

Safety Hour Attendance Last Week – 80%  (Target = 67%)

Close Calls Raised – 35  (Target = 58)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

28/06/2017
02:10
Ludgershall
Staff accident
Two members of Salisbury PWay believed they were stung by wasps.
They stopped work and left the area.
One had been stung on the bridge of nose and the other on the right armpit.
The Golden Hour was applied and there was no lost time.
28/06/2017
13:45
Warblington
Accident Report
A member of Havant S&T was tucking signal cabling into a troughing route using a Lid Lifter when a shard of fibre glass came off of the shaft, passed through the glove and impaled into the skin area between the left thumb and finger.
First aid was given on site and the inch long shard was removed by the Team Leader.
The Golden Hour was applied and no time was lost.
30/06/2017
09:15-13:26
Worting Junction
Alleged Staff near miss
An alleged near miss occurred on a bridge structure with a member of Basingstoke S&T whilst investigating a fault on BE183 signal.
The Lookout had given a warning, but the COSS believed that he was in a position of safety within 7 seconds of the train passing.
Chain of care was carried out on all staff and this incident is subject to further investigation.
30/06/2017
16:17
Guildford
Staff Accident
An E&P Manager reported a minor RTA whilst driving out of Ludlow Road onto Guildford Park Road into traffic when he did not notice an oncoming vehicle.
No damage or injuries were sustained when his front tyre rubbed against the other vehicles near side bumper.
The Golden Hour was applied mainly for chain of care, as no injuries were sustained.
02/07/2017
06:05-08:23
Bracknell
Possession irregularity – Item 113
A COLAS rail grinder 6Z08 was authorised out of a Worksite having completed its work and was making its way to detonator protection to exit the T3 possession, but the PICOP had not been asked permission for this movement to take place.
In addition to this, Crossing Attendant that had been booked on to manage the barriers between Bracknell and Wokingham also allowed the train to continue by carrying out his duties without the PICOP having advised him to do so.
This incident is subject to further investigation.
02/07/2017
23:42-01:21
Waterloo
Lighting Rig knocked over by RRV
A Works Delivery Manager reported that an RRV within the T3 possession had knocked over a lighting tripod which had then fallen onto a live conductor rail floater.
The strike caused a flashover and scorch damage.
The Manger believed that the conductor rail concerned should have been isolated and raised a concern that staff have been stepping over the rail concerned carrying tools and had fuel stored alongside the rail.
The Operations Delivery Manager and Engineering Supervisor confirmed that as far as the live floater was concerned, an irregularity had not occurred as some floaters where points are concerned are to be considered to be live unless tested locally.
The issue was referred back to the Planning team to establish is any alterations could be made to mitigate against this.
The incident involving the tripod is under further investigation.

Material

Safety Bulletin – Detonators

IP Southern Home Safe 28 June 2017

Safety Hour slides-Minor Works-Ioannis-June 2017

Validium Change Poster July 17

Validium Newsletter July 17

Validium Change Info Sheet July 17

HAVS Tier 3 Clinics:
All Wessex Line Manager from Works Delivery and Maintenance who have employees identified as requiring  the Tier 3 HAVS Surveillance programme will receive an automated email from OH Assist.  As Line Manager this is only to make you aware that your employee/s have been referred.  You have to take no further action at this time.  If however, the information is incorrect (i.e. the employee doesn’t work for you any longer; has left Network rail or haven’t used vibrating tools for more than 2 years) then please contact grazia.elsehimy@networkrail.co.uk as well as NWRhealthsurveillance@ohassist.com to inform them of the error.

 

If you would like to raise a question about this call. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

A recording of this call can be found below:

If you are having problems with the player above, please click here.

Wessex Safety Hour – 27th June 2017

Safety Hour Attendance Last Week – 71%  (Target = 67%)

Close Calls Raised – 35  (Target = 58)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

20/06/17
Holton Heath
Road Traffic Accident
Two members of Bournemouth S&T experienced a Road Traffic Accident whilst going round a roundabout when a car pulled out from the left-hand side.
The car struck the rear of their van, but there were no injuries.
The Golden Hour was applied.
25/06/17
Waterloo
Staff Accident (assault)
A member of Network Rail station staff confronted a well-known beggar in Burger King about begging on the station and asked him to leave.
The beggar raised his fists up to them and was restrained to the ground after the staff member felt threatened.
A SWT Driver saw the incident and assisted the member of station staff until BTP arrived.
The Golden Hour was applied.

Material

If you would like to raise a question about this call. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

A recording of this call can be found below:

If you are having problems with the player above, please click here.

Wessex Safety Hour – 20th June 2017

Safety Hour Attendance Last Week – 78%  (Target = 67%)

Close Calls Raised – 37  (Target = 58)

% of Close Calls in <90’s – 91%  (Target = 85%)

 

Incidents last week

12/06/2017
Byfleet and New Haw
Line side fire
4Y19 reported a line side fire on the Down cess near signal WK549.
Upon the MOM arriving, the fire had spread and covered 50 yards of the embankment.
By 17:14 the fire was out after the fire brigade attended.
The cause was felt to be connected to a tin can or a piece of metal foil that had come into contact with the conductor rail.
Please be aware that in dry conditions it can assist the acceleration of a fire, so be mindful the combustible materials that are around us.
A fire can start from a spark from a train pick up shoe or a discarded cigarette, so please look for the risks that are posed to us and report or remove them.
Remember to make use of the Close Call system too.
14/06/2017
Southfields
Cat A Spad 2174
A London Underground District Line service had a Cat A SPAD at W367 signal.
The Driver made no allegation against the signalling and stated that they had a loss of concentration.
This incident will be subject to an LUL investigation.
13:11-19:15
Eastleigh East Yard
Derailment
Balfour Beatty reported that one axle had derailed involving a Tamper on the Crain Pit Road over CJ points.
The Track Section Manager reported that there was no flange climb on the switch rail, but it had appeared that the front wheels had split the points and the axle that derailed ran down the back of the switch to the point of derailment.
There was some damage to the tips of the switch rail.
This incident shall be investigated by the Yard owner.
16/06/2017
Fratton
Cat A SPAD 2E64
South West Trains service 2E64 reported a Cat A SPAD at HT60 signal on the up main.
The Driver made no allegation against the signalling and stated that they had a loss of concentration.
This incident is subject to a review and follow up investigation.
17/06/2017
Pirbright Junction – Woking Junction
Possession Irregularity Item 35
Train 3Z10 reported to the Signaller that they had come to a stand at a stop board with detonators on the Up Fast Line.
Upon investigation it was established that a Vital Possession Support Staff (PSS) contractor had placed the protection incorrectly leaving the down fast unprotected.
This incident is subject to a Level 1 investigation.
The PSS had been briefed prior to applying the protection, but early indications show that there was a possibility that they had become disorientated with the layout once on site.
17/06/2017
Totton
Rough Ride / Rail Buckle
South West Trains service 1W65 reported a rough ride / kink in the rail at 573 points on the down line country side of the station which resulted in the line being blocked.
Upon the PWay attending a known location for rough rides, they noted a slight dip and authorised normal working. This was not the area where the defect was.
Once opened at line speed, 1W25 travelling at 65mph reported another jolt on the left hand rail of the down main on or near E577 points, a further train was cautioned and reported that the defect was very bad. The line was blocked until it was rectified overnight.
Early indications show that communications may have become confused and assumptions were made which took the PWay to the wrong location.
This incident is subject to a review and further investigation.
17/06/2017
Hook
6N01 Load Moved
6N01, the 1200  Vauxhall – Eastleigh East Yard reported that they had felt the load move.
The train had been within a Wessex Capacity possession and the load consisted of old track still fastened to their sleepers.
The load had been checked before it had left site by a Load Examiner.
The train stopped by BE401 signal between Hook and Basingstoke and the down lines were blocked due to the load now being out of gauge.
Upon a further examination by the Driver and Load Examiner (who had also checked the train earlier) it was identified that a strap was missing allowing the load to shift.
The down lines were affected for 3 hours until the train was safely recessed and dealt with at Basingstoke.
This incident is subject to further investigation.

Material

Management of Occupational Road Risk NR:L1:OHS:210
IP Home Safe 14 June 2017

If you would like to raise a question about this call. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

A recording of this call can be found below:

If you are having problems with the player above, please click here.

Wessex Safety Hour – 13th June 2017

Safety Hour Attendance Last Week – 57%  (Target = 67%)

Close Calls Raised – 37  (Target = 58)

% of Close Calls in <90’s – 92%  (Target = 85%)

 

Incidents last week

04/06/2017
Kew Bridge
Staff Accident
A PWay Team Leader was walking along the cess when some loose ballast gave way twisting his left knee.
An ice pack was used to reduce any swelling and the Golden Hour was applied.
This incident did not result in any lost time.
04/06/2017
Eastleigh Pre-Assembly Depot
Derailment
DB Cargo reported that a Coalfish wagon had become derailed between 4 and 6 Road over a set of hand points whilst carrying out a shunt move.
Upon examination by Network Rail PWay (who patrol, but are not responsible to maintain), they found that there had been 3 to 4 sleepers replaced consecutively after a previous derailment, but not packed.There was also evidence of soil / sand being used and not ballast.The incident was subject to a DB Cargo investigation and Network Rail patrolling responsibilities were visited.
06/06/2017
Sunbury
Staff Accident
A member of Feltham S&T was driving along a road in Sunbury when a the car in front braked to turn into a driveway.
The S&T Driver went to brake themselves, but their foot slipped off the peddle resulting in a low speed collision between 5 to 10mph.
There were no injuries sustained to either party and no apparent damage to the vehicles.
The Golden Hour was applied and there was no lost time.
06/06/2017
Tisbury
Late Acknowledgment of train horn
1L37 reported that a track worker did not acknowledge the train horn until the 3rd time of sounding it.
The Driver did not declare the incident as a Near Miss.
09/06/2017
White Hart Lane Level Crossing
Level Crossing Irregularity
The Signaller on Wimbledon Panel 5 lowered the crossing and cleared an Up line signal for train service 2U22 to proceed.
Upon doing so, they had realised that they had trapped a member of the public within the crossing next to the Up side Facing barrier and corrected their error by making an urgent call on the GSMR to the driver and replacing the signal to danger (red).
Once the signal timed out, the barriers were raised and the member of public released.
This incident is subject to further investigation.
09/06/2017
Eastleigh
Staff Accident
Upon carrying out de-vegetation work at the Electrical Control room, a Ground Control contractor noticed 7 ticks on his body.
Having been trained to do so, the ticks were removed safely.
Ground Control followed the incident up and there was no lost time.
10/06/2017
Barnes / Feltham Junction
Possession Irregularity – Item 115
Whilst travelling on a passenger train at approximately 14:54hrs, a member of Feltham PWAY noticed that the protection for the T3 possession may not have been applied correctly in the Hounslow / Whitton Junction area.
Upon the Operations Delivery Manager (ODM) attending site, it was identified that an irregularity had in fact occurred and that the detonator protection was placed 7 chains out of position and beyond the Work Site marker board.
The protection had been like this since approximately 01:16hrs.The ODM corrected the error made and arranged a follow up investigation into the incident which had involved McGinley contract staff.
Many thanks to the member of Feltham PWay staff for noticing and reporting this.

Material

Means Health Week 2017 – Info Sheet
Means Health Week 2017 – Waist

If you would like to raise a question about this call. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

A recording of this call can be found below:

If you are having problems with the player above, please click here.

Wessex Safety Hour – 6th June 2017

Safety Hour Attendance Last Week – 63%  (Target = 67%)

Close Calls Raised – 31  (Target = 58)

% of Close Calls in <90’s – 93%  (Target = 85%)

 

Incidents last week

8/05/2017
Portsmouth and Southsea
Staff Accident
A member of Havant S&T cut their left hand index finger.
First aid was given and they attended a walk-in clinic.
The Golden Hour was applied and this was not a lost time injury.
29/05/2017
Havant
Brake Failure on a Road Railer
Whilst a Road Railer was being driven back from Witley to Havant, its brakes failed approaching a roundabout resulting in the vehicle going straight across it.
Apart from the Driver being in shock, no injuries were sustained.
The Golden Hour was applied and there was no lost time.
29/05/2017
Portcreek Junction
Worksite Irregularity
The Section Supervisor for Inner distribution (On Call) advised that he had been informed that Works Delivery staff had been working on point heating equipment whilst being live within T3 item 62.
Works Delivery do not hold this competency.
The Section Supervisor made the area safe by cutting out the electrical supply to the strips and would reconnect at a later date.
The incident was Close Called and is subject to further investigation.
30/05/2017
Surbiton
Staff Accident
An Inner Assistant Track Section Manager was changing trains at Surbiton and boarded a very crowded train.
Another passenger got on and pushed into their bag twisting it around and forcing their left shoulder into a hand rail.The Injured Party had an existing rotator cuff injury which was expatriated by the action.
The Golden Hour was applied.
02/06/2017
New Malden
Staff Accident
Upon the completion of works within a T3 possession and loading grinding equipment on the back of a van, a Welding Team Leader trapped his left hand causing some swelling and bruising.
The Golden Hour was applied and this was not a lost time injury.
04/06/2017
Kew Bridge
Staff Accident
A PWay Team Leader was walking along the cess when some loose ballast gave way twisting his left knee.
An ice pack was used to reduce any swelling.
The Golden Hour was applied and the Injured Party was due to see his GP on Monday (05/06/17) morning.
This was a lost time injury.
04/06/2017
Eastleigh Pre-Assembly Depot
Derailment
DB Cargo reported that a Coalfish wagon became derailed between 4/6 Road over a set of hand points during a shunting movement.
The PWay who patrol, but do not maintain the area reported that 3 or 4 sleepers had been replaced consecutively recently by an outside party,  but had not been packed. There was also evidence of soil/sand being used rather than ballast.
It was therefore believed that the area had been loose enough to allow the waggon to move causing the derailment.

Material

IP Southern Home Safe 31 May 17
London Bridge – Stakeholder Briefing – 4 June 2017

If you would like to raise a question about this call. Please feel free to comment on this post and it will be answered as soon as possible. If you would like to remain anonymous, please state in your comment and it will not be published.

A recording of this call can be found below:


If you are having problems with the player above, please click here.